Ongoing Work 2021
April

April 14/15th - Head Gasket and Pedal Spring Replacement

For a while, I've suspected a head gasket leak on the GPW. Coolant level was dropping, the radiator overflow was blowing coolant and the engine sounded lumpy at start up. When I changed the oil, just before moving house, there was a little water in the sump. The first thing I did was drain the oil and coolant. With the radiator empty, I fitted a new drain cock as the wings on the old one were damaged. Next job was to remove the oil filter and the radiator hose, then I could unbolt the cylinder head.
  

 
I found my cylinder head leak between cylinders 3 and 4. I ordered a new gasket and set about to change it on April 14th. That's when it got frustrating. When the engine was rebuilt, I knew that bolt number 1 was stripped in the block. I understood from the engine rebuilder that he tapped a new larger thread in the block and put a bigger bolt in. However, once the head was off, it was clear he didn't bother. What he did do was to tap the cylinder head and put a bolt in, giving the impression it was tightening up on the block when all it was actually doing was filling the hole in the head.
 
 
The engine is old, pre-war in fact and isn't the greatest. I didn't fancy trying to cut an even bigger thread in the block, which would also require the head being drilled out. Equally, I didn't want to put a helicoil in, since the already oversized hole was so close to the water passage. My solution was to drop a large nut and washed down the cooling passage, attached to cotton. A threaded rod was coated in epoxy and passed through its hole before being screwed into the washer and nut. Effectively the block now has a permanent stud. Another nut was fastened on overnight to hold it vertical while the epoxy cured.
 
On the 15th, the gasket was fitted and head bolts torqued up, nipping up the nut on the new stud at the same time. Once back together, I gave it a run, but got some weeping passed the threads in the new stud as it was a bit smaller than the head hole and the washer on top wasn't making a good seal. Like on the rear crank bearing seal, I made a mini rope seal soaked in gasket seal which was pushed down around the stud. A plastic crush washer was next, then a metal washer and nut. That seemed to fix it. It's a bit of a bodge, but I felt this was the least destructive way of sorting the problem and something that is reversible. It's got to be better than not being bolted down at all.
 
Before the first start, I turned the engine over on the starter to pump some oil and coolant around the engine. Then I was started ( see the video below ). It was run to temperature, cooled and re-torqued, then run again and re-torqued. I had a bit of a dash up and down the drive to put it under a bit more load and it is now cooling down again for another re-torque. I'll do another proper test drive tomorrow once Lynne is here so I have recovery assistance.
 
 
While tinkering, I also fitted a new clutch pedal and brake pedal spring. The old ones didn't have much spring left in them, giving a very limp clutch pedal.
 

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